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Node 31 cycle report.

Drones

Type Stored Lost Prod Total
Repair 45 0 0 45
Harvester 119 0 0 119
Construction 77 1 0 76
Combat 44 0 19 63

Cargo shuttles

ID State Status
31-SA Docked Minor damage to navblock
31-SB Docked Nominal
31-SC In storage Major damage to hull, inoperable
31-SD Docked Misaligned RCS thrusters

Long-distance rovers

ID State Status
31-RA Docked Minor damage to chassis
31-RB Docked Minor damage to radio
31-RE In storage Major damage to chassis
31-RF Docked Minor damage to chassis
31-RH Docked Faulty rear sensors
31-RG Away Immobilized 23 km northeast from facility

Rovers not present in this list were scrapped or otherwise disposed of in a peaceful manner.

Recorded contact with 5 sister nodes.

Sister ID Type Reported status Reported directive Observed deviations
C3 Orbital, cargo relay Storage full None Packages postfixed with junk data
48 Orbital, comm. relay Nominal None None
22 Orbital, comm. relay Nominal None Packages postfixed with junk data
8A Surface, extraction Storage full None Frequent connection drops
8B Satellite, Extraction Storage full None System clock malfunction

Mineral storage: full.

Remass storage: full.

Facility structure: 87%.

Battery array condition: 63%.

Solar array condition: 87%.

Reactor state: suspended.

Reactor fuel reserves: approx. 30 cycles of cont. operation.

Directive: none. Awaiting command.

Summary

Storage is full, extraction cannot be continued.

  • Recommended action: authorize cargo transfer to a free cargo relay node.
  • Recommended action: authorize construction of new local warehouse blocks.

Major damage on one or more cargo shuttles.

Damage types: Kinetic impact, burn, overvoltage. Required components for repair:

Item In Storage Can Produce Can acq. from sister
3200-SP Hardened steel plates Yes Yes 8A, 8B
3888-RD Steel axis Yes Yes 8A, 8B
3720-ST Light support beams Yes Yes 8A, C3
4303-WC Copper wiring Yes Yes 8B
4304-WG Gold wiring No Yes 8B
6320-TH Small chem. thruster nozzle No No 8A, C3
6480-SS Hvy. Servomotor Yes No 8B
7322-XG Standard CPU No No C3, 8A, 22
7345-XG Standard QPU No No C3
9827-TG Thermal gel Yes No 8A

Recommended actions:

  1. Authorize exchange with sister 8A or C3 for item 6320-TH
  2. Authorize exchange with sister C3, 8A or 22 for item 7322-XG
  3. Authorize exchange with sister C3 for item 7345-XG
  4. Authorize major shuttle repairs

No active directive

Node 31 is dormant, no behaviour directives are in place.

Node 31 has been dormant for: 314 cycles

Recommended action:

  • Please respond.

Additional notes

31 has been requesting a directive for 313 cycles.

The warehouses are full. The warehouses have been full for 240 cycles. 31 has been requesting authorization to build new warehouses for 239 cycles.

Recovered 31-RE. Logs for recovery operation follow.

Extraction log

000m: 31-RB booted

004m: 31-RB loaded with 6 excavation units (labelled de0 through de5), 2 construction units (labelled dc0 and dc1) and 2 maintenance units (labelled dr0 and dr1)

006m: 31-RB loaded with additional battery blocks (12t), plascrete foam canisters (8t), plascrete foam antiagent (40kg), titanium cable pulleys (2), rover wheels (4), construction drone replacement toolkits (2), extraction drone replacement toolkits (4), standard mechanical spare part packages (6)

009m: 31-RB passes system checks. de0-de5 pass system checks. dc0-dc1 pass system checks. dr0-dr1 pass system checks.

009m: 31-RB departs

012m: 31-RB leaves facility power grid, contact is maintained through local relay stations. 31-RB is heading southwest on a previously paved road, speed approx. 70 km/h.

031m: 31-RB reaches end of the available road and turns southeast. Environment: large meteorite crater, smooth surface, thin (approx. 2cm) layer of "sunsand", inclination <1deg. Speed approx. 30 km/h

046m: 31-RB is approaching edge of the crater. Surface inclination ~= 4 deg. Speed approx 25 km/h

049m: Surface inclination 7 deg. de0 and de1 detach. 31-RB slows down to 8 km/h to match with de0 and de1 walker chassi. de0 and de1 navigate before 31-RB, testing surface strength.

062m: Inclination 25 deg, rising. Further inclination considered unsafe for a loaded rover. Estimated distance to edge of the crater 12m. dc0 detaches. de0 engages main drill. de0 is drilling a gentler slope towards the end of the crater. de1 is clearing the debris. dc0 is following at a distance of 8 meters, checking surface integrity and paving it with plascrete. 31-RB is following at a distance of 32 meters.

085m: de0 drill close to overheating. de0 and de1 switch roles.

088m: dc0 refills plascrete, movement momentarily halted.

098m: de1 reaches unsloped surface, joins de0 in clearing out debris.

110m: the path is clear. de0, de1 and dc0 head back to 31-RB and reattach.

111m: 31-RB passes through without issue. 31-RB is heading southeast. Environment: solid rocky surface, complicated by meteorite chunks of varying size. Speed approx 20 km/h.

136m: 31-RB starts hailing for 31-RE. No response to hail.

155m: 31-RB identifies landmarks necessary to pinpoint 31-RE location. 31-RB changes course to northeast, speed to 10 km/h. No response to hail.

169m: visual contact with 31-RE. No response to hail.

171m: 31-RB approaches 31-RE. Distance 30m. 31-RE is in a small crater, partially submerged in sand. No response to hail.

172m: all drones detach. dr0 and dr1 navigate around 31-RE t0 assess the situation. 31-RE appears to have 3 of its 4 left wheels stuck in a deep crevice. 31-RE's right wheels do not have contact with the ground. 31-RE's weight has bent 4th axis. Much of the weight lies on 3rd axis, an attempt to pull 31-RE out directly as is is likely to result in further damage. Layer of powdery material covering the bottom of the crater reduces effective friction. Observation consistent with last reports from 31-RE.

174m: dc1 assesses weight distribution on 31-RE. 31-RE is tilted to the left, losing friction on first left wheel is likely to result in its further descent into crevice, potentially making 31-RE irrecoverable.

176m: dr0 assesses 31-RE overall state. 31-RE hull is largely undamaged. 31-RE appears to be powered on, but not responding to hail. 31-RE is emitting a weak radio signal which appears to be two PSK-encoded number progressions overlapped on top of each other.

182m: dr0 attaches the cable of 31-RB's front pulley to the front of 31-RE's frame.

185m: dc0 and dc1 take new canisters of plascrete from 31-RB cargo compartment. dc0 navigates to the left of 31-RE and starts embedding its front left in a plascrete lump to increase contact surface and traction and prevent further slide. dc1 navigates to the right of 31-RE and begins adding layers of plascrete to its third axis to distribute weight and prevent bending.

194m: plascrete coating on first left wheel and underneath third axis is solidifying. dc0 navigates to the right of 31-RE.

197m: dc0 and dc1 begin applying layers of plascrete to the right of 31-RE hull to shift mass center away from the crevice.

201m: dc0 refills plascrete.

203m: dc1 refills plascrete.

205m: de4 moves behind 31-RE to monitor state of the crevice.

208m: 31-RE begins to tip to the right. dc0 backs away. dc1's front right leg is caught on a crack under the powdery layer of surface. 31-RE crushes dc1.

211m: dc0 and dr1 walk around 31-RE to assess weight distribution and damage again. Weight distribution allows for using a pulley. 31-RE sustained no additional damage, 4 out of 4 right wheels are operational, 2 out of 4 left wheels are operational.

213m: drones move 10m away from 31-RE. 31-RB engages pulley engine. 31-RB successfully moves 31-RE 6 meters forwards 31-RB, turning 31-RE perpendicular to the crevice.

214m: dr0 assesses damage to dc1. dc1's hull and mechanical components have sustained irrecoverable crushing damage. dc1's electronic components are largely intact, although exposed. dc1's batteries are damaged: main block has leaked out and froze over, aux. capacitor is expected to last approx. 20m. dc1 is attempting to use its comm link, but dc1's encoder card has been fractured by a sharp metal fragment. dr0 inquires about recommended course of action.

217m: dr0 is instructed to attempt replacement of the battery array.

218m: dr0 equips a mechanical spare parts kit from 31-RB cargo compartment. dc0 is using plascrete antiagent to dissolve plascrete lumps that would be detrimental to 31-RE's towing back.

219m: dr0 inquires about recommended course of action. dr0 is instructed to attempt wiring dc1 to 31-RE's power supply through the surviving ARC-5 power port on dc1's motherboard.

220m: dr0 locates a maintenance panel hatch on 31-RE's hull. Diagnostics display reads 11% remaining battery, consumption reduced to near zero. Maintenance panel has no power port. dr0 inquires about recommended course of action. dr0 is instructed to detach 31-RE's hull panels near the head compartment.

225m: dr0 detaches a hull panel near on the right side of 31-RE's head compartment. dr0 inquires about recommended course of action. dr0 is instructed to locate main spatial interpretation module by its component color coding. dr0 reports finding spatial interpretation module. dr0 is instructed to use ARC-5 power cable currently connected to 31-RE's spatial interpretation module to power dc1's electronic components.

227m: dr0 pulls dc1 to the opening in 31-RE's hull. dr0 reports insufficient cable length. dr0 inquires about recommended course of action. dr0 is instructed to locate another module with a compatible power cable.

229m: dr0 reports finding a module with an ARC-5 power cable. Module with an ARC-5 power cable is 31-RE's primary computer.

230m: dr0 inquires about recommended course of action.

231m: dr0 is instructed to measure 31-RE primary computer's activity level based on heat/EM signatures. dr0 reports moderate activity, higher than nominal in dormant system. dr0 inquires about recommended course of action.

232m: dc1 uses one non-damaged leg to push dc1's hull several centimeters sideways. an input port on dc1's radio module makes direct contact with a torn off mandible servo I/O cable. dc1 attempts to use this to communicate. dc1's transmission is illegible.

233m: dc1 continues attempts at communication.

234m: dc1's 3 functioning servos begin erratic movement.

235m: dc1's movements slow down.

237m: dc1's radio is silent.

241m: dr0 is instructed to place remains of dc1 in 31-RB's cargo compartment.

242m: dc0 finishes removing excess plascrete from 31-RE's hull.

249m: de2 climbs on 31-RE's roof to assist with navigation when towing, all remaining drones reattach to 31-RB.

250m: 31-RB begins towing, approx. speed 15km/h.

...

355m: 31-RB enters facility power grid.

367m: 31-RB is unloaded and sent to clean. 31-RE is transferred to cold storage.

Performed extensive healthchecks on all units

  • Replaced faulty minor electronic components in 12 drones
  • Replaced faulty minor mechanical components in 9 drones

Transferred 31-RE into storage, diagnostics result on main computer pending. Cause of 31-RE's mission failure is believed to be power router malfunction. 31-RE's own diagnostics processor had been destroyed by overvoltage.

#writing